thewayne: (Default)
So on top of its aircraft troubles, and its spaceship trouble, oh - did you hear they have an on-going strike, now they have had a satellite explode in space! (the strike is in its sixth week and workers (jet assembly line) voted to reject Boing's most recent offer) Boing just announced a $6 billion quarterly loss last week

So. The satellite. The Intelsat 33e was launched in 2016 and experienced "an anomaly" Saturday, and is now in 20 trackable pieces, and who knows how many smaller ones according to Space Command, Roscomos says they're tracking 80, and the major debris does not represent a threat to other satellites. These huge satellites are normally in much higher geostationary orbits so the debris is a very different field than if they were in lower orbits.

Its job was to provide communications across Europe, Asia, and Africa. Boing is working with other satellite vendors to reestablish services for its customers.

https://www.cbsnews.com/news/boeing-satellite-intelsat-33e-explodes-space-anamoly/

https://tech.slashdot.org/story/24/10/24/0142204/boeing-made-satellite-explodes-in-space

Strike news:
https://apnews.com/article/boeing-earnings-strike-vote-new-ceo-af6c6dab8747d5b8189df97a55e6b8d9
thewayne: (Default)
Its return was successful. That's the good news, but the flight was not without incident: "Flight controllers conducted more test firings of the capsule’s thrusters following undocking; one failed to ignite. Engineers suspect the more the thrusters are fired, the hotter they become, causing protective seals to swell and obstruct the flow of propellant. They won’t be able to examine any of the parts; the section holding the thrusters was ditched just before reentry."

So they've recovered the capsule, and now they have a theory about what caused the thruster malfunction. And it's not difficult to test thrusters under high temperature as they have test chambers that can easily simulate those conditions. So we may have some answers on the thrusters forthcoming.

But we still don't know about the helium leak. Helium is kinda tricky. It's a very small molecule and can leak easily, that's why rubber helium balloons shrink so rapidly. The mylar helium balloons keep their inflation because mylar is less leaky than rubber: harder for the gas to escape.

Included in the capsule were the two astronauts' space suits and some old lab equipment.

The article has a video of the capsule undocking from the ISS which is pretty cool, seeing the thrusters firing to change its orientation.

https://www.huffpost.com/entry/astronauts-left-behind-boeing-starliner-capsule-returns_n_66dbe6e5e4b01c1d24fc405c
thewayne: (Default)
The noise is described as like a sonar ping. Clearly it has reverted to P-3C Orion mode and is hunting for Nazi submarines from a better vantage point. What it's going to attack with if it finds any, I'm not sure.

The cause is most likely benign, however, with Boing these days, you can't be too careful. Spacecraft have a history of odd, benign noises. From the article: "Astronauts notice such oddities in space from time to time. For example, during China's first human spaceflight int 2003, astronaut Yang Liwei said he heard what sounded like an iron bucket being knocked by a wooden hammer while in orbit. Later, scientists realized the noise was due to small deformations in the spacecraft due to a difference in pressure between its inner and outer walls."

https://arstechnica.com/space/2024/09/starliners-speaker-began-emitting-strange-sonar-noises-on-saturday/
thewayne: (Default)
The software has been updated for Boing to take full remote control of the vehicle and attempt to undock it and bring it back to Earth, where it will land at Space Harbor at White Sands Missile Range, about a hundred miles from my house, around six hours later. If all goes to plan.

One disappointing thing about it is that the thrusters that are the center point of the problem will be lost. Once the capsule is properly oriented for atmospheric reentry, they are part of an assembly that is ejected from the craft and they burn up in the atmosphere. We'll never know precisely what was wrong with those helium thrusters and we'll have to hope that engineers can duplicate the problem with ground-based units and testing.

https://arstechnica.com/space/2024/08/boeing-will-try-to-fly-its-troubled-starliner-capsule-back-to-earth-next-week/

White Sands is a tough place. It is the world's largest gypsum desert, pull it up in Google Earth, it's pretty cool. Once the Space Shuttle landed in California at Edwards and was being flown back to Florida and landed at White Sands to avoid a storm. And the gypsum just utterly trashed the 747 transporter's brakes! It was supposed to be there for a day or two while the storm abated, it was there for a couple of weeks while a crew was brought out to check out and service the plane! But it was a very scenic backdrop for photos while it was there.


The Dragon capsule that will be flying in late September with Crew 9 has had the final crew decided. The crew has been reduced from the normal four to two to accommodate the return of the two astronauts stranded by Boing. The capsule has been modified with additional seats behind the four crew seats.

One issue has been that of space suits. NASA standard space suits, such as those used for the travelers in the Starliner, are not compatible with the fittings in the Dragon. SpaceX has much more modern suits which are more comfortable and flexible/maneuverable for travel, whereas the NASA suits are better for EVA work if needed. There is one spare SpaceX suit on-hand on the ISS right now that will fix one of the two stranded astronauts, NASA has not revealed which. And Crew 9 will be bringing another suit, presumably for the other astronaut, so everyone will be properly suited for their return in February.

There is a second purpose for the seat reconfiguration of the Dragon capsule. The norm for the ISS is that there is always a Soyuz capsule docked to be used as an emergency life boat in case the station has to be abandoned in the event of an emergency: a fire, a debris collision that can't be avoided, etc. There have been a few times over the station's life where the crew have taken shelter in the capsule. This seat reconfiguration will allow the Dragon to serve as a lifeboat while docked. I have no idea if the Russians are planning a launch to coincide with the departure of the Dragon in February to fill its emergency role.

https://arstechnica.com/space/2024/08/nasa-makes-a-very-tough-decision-in-setting-final-crew-9-assignments/
thewayne: (Default)
I could spew an absolute ton of invective right now.

That shitshow of a capsule called the Starliner should not have launched. They knew there were problems with those thrusters, and they had problems docking.

And the problems have gotten worse.

The two astronauts were supposed to be up there for two weeks, then return home. They've been up there for TWO MONTHS. And now there's some very hard problems, and they could potentially result in fatalities.

Here's the basic problem. A spaceship contains batteries. The batteries have a fixed lifespan. The batteries in the Starliner are rated through the end of August. That's not much time.

NASA is not 100% confident that the thruster problem is resolved. But Boeing is. Everybody raise your hands and jump up and down if you trust Boeing's answer.

Now, the previous successful mission of the Starliner worked great. Unmanned, it was launched, flew up to the ISS, docked itself, then later uncoupled, de-orbited, and landed in the ocean and was recovered. So the obvious answer is, why can't they do that, and the two astronauts be returned on a later flight?

BECAUSE BOEING REMOVED THE FUCKING SOFTWARE THAT PERFORMED THAT FUNCTION.

They updated software that worked. The big question is whether or not NASA and the two astronauts were notified of this change. Now someone, or some two, will have to be in that capsule, with potentially twitchy thrusters, to decouple it from the ISS and attempt to fly it back home.

The thrusters are needed twice. To move the capsule away from the ISS - SAFELY - and to reorient the capsule for its de-orbit burn. If the de-orbit burn is not performed correctly, it can mean quite literal death for the capsule occupants. And the thrusters are not 100% reliable.

I am absolutely flaming furious at Boeing!

Yes, space is hard. That's why engineers are careful and try to make sure everything is done right BEFORE any vehicle is classed as flight capable. This damn Starliner should never have been launched, it was scrubbed once because the thrusters were leaking, they should have scrubbed it again until they thoroughly understood what the problem was and it was absolutely fixed.

People's lives depend on it, you don't fuck around.

https://arstechnica.com/space/2024/08/nasa-likely-to-significantly-delay-the-launch-of-crew-9-due-to-starliner-issues/
thewayne: (Default)
One complaint that investigators into Boeing's systems after the plug blow-out was that there didn't seem to be any paperwork regarding repairing the door. Suspicions were raised that Boeing or people on the shop floor deleted said records, but 'we the people' never really heard the resolution of this.

Now a Boeing executive is saying there was no paperwork because the door plug repair was not assigned to a repair team! Now, obviously that demonstrates a problem. Why was no ticket issued? Inquiring minds want to know!

We may have an explanation: " Boeing said during the Tuesday briefing that the reason the Alaska Air door plug was not probably secured in the first place was because two different groups of employees at the plant were charged with doing the work, with one removing and the other reinstalling the door plug as the plane was passing along the assembly line.

The first group of employees removed the door plug to address problems with some rivets that were made by a supplier, Spirit AeroSystems. But they didn’t generate the paperwork indicating they had removed the door plug, along with the four bolts necessary to hold it in place, in order to do that work.

When a different group of employees put the plug back in place, Boeing says the employees didn’t think the plane would actually fly in that condition.

Instead, they were just blocking the hole with the plug to protect the inside of the fuselage from weather as the plane moved outside to a different area of the factory compound. That group of employees often makes those kind of temporary fixes.

“The doors team closes up the aircraft before it is moved outside, but it’s not their responsibility to install the pins,” said Elizabeth Lund, senior vice president of quality for Boeing’s commercial airplane unit. "


But there's a bigger problem. :-)

This is a Federal investigation by the NTSB. Boing isn't supposed to say 'boo' unless it is cleared with the NTSB for release. They don't want any information being released until it's reviewed and approved, they want anything released to be as truthful as possible.

Care to guess what the Boing exec who released this information didn't do?

And the consequences are pretty grave for Boeing. "The NTSB said that given its recent actions, Boeing won’t have access to investigative information the agency produces about the Alaska Airlines incident, but it will keep its party status to the investigation.

The NTSB is unable to fine Boeing, as it doesn’t have enforcement authority. While the agency could have stripped away Boeing’s party status, the NTSB may have considered it more important to keep Boeing as a party to the investigation because of its employees’ expertise.

The NTSB said that it may subpoena any relevant records it requires during the course of the investigation. It also will subpoena Boeing to appear at an investigative hearing in Washington D.C. on Aug. 6 and 7. The agency said that, unlike other parties, Boeing won’t be able to ask questions of other participants."


Boeing knew the rules of an NTSB investigation as they've been party to quite a few of them. There's really no excuse for this kind of stupidity. This might be an executive resume-generating event.

https://www.cnn.com/2024/06/27/business/boeing-cause-alaska-air-door-plug

https://www.huffpost.com/entry/boeing-sanctioned-sharing-737-max-9-investigation-info_n_667d5231e4b07cb66c6d070b
thewayne: (Default)
No, a Dutch roll isn't a weird sex position. Well, it probably is, but we won't get into that. In an aircraft, it's an uncontrolled side-to-side yawing motion of the tail, and it can be lethal: a 747 experienced that and crashed, killing most all on board. In this case, the plane, less than two years old, experienced it after taking off from Phoenix. The pilots were able to regain control and landed safely. A subsequent investigation found a damaged backup power control unit, which is responsible for power to the tail.

If a Dutch roll is not controlled by the flight crew, it can cause the tail to shear off or otherwise fail catastrophically.

The plane was grounded for several days and then flown to Everett, Washington where one of the airline's major maintenance vendors is located. Reportedly no one was seriously injured in the incident, though many were violently ill.

https://www.npr.org/2024/06/13/nx-s1-5004725/boeing-737-max-southwest-dutch-roll

https://news.slashdot.org/story/24/06/14/0331240/faa-is-investigating-new-incident-involving-a-boeing-737-max-8-jet-in-midair
thewayne: (Default)
The jet cleared the end of the runway with just under 300 meters remaining and sailed over the A38 (major highway) with 30 meters of clearance!

The culprit? Something called Auto-Throttle. The pilots, per standard procedure, set the take-off thrust to 92.8%. Then somehow the plane dialed itself down to 84.5%, giving it a take-off speed of about 150 knots, which isn't very much.

During the subsequent investigation, "Boeing told investigators looking into the incident that they were aware of a “long history of nuisance disconnects during takeoff mode engagements”."

Uhhh.... you're aware of a "LONG HISTORY OF NUISANCE DISCONNECTS" and you haven't fixed it?!!! WTF?!!!

The article goes on to relate the incident in April of a FedEx cargo plane landing in Turkey WITHOUT THE FRONT LANDING GEAR DEPLOYED! It somehow managed to stay on the runway and stop safely.

https://www.independent.co.uk/travel/tui-boeing-flight-bristol-disaster-avoided-b2558536.html

https://tech.slashdot.org/story/24/06/07/2032214/boeing-passenger-jet-nearly-crashes-due-to-software-glitch
thewayne: (Default)
*sigh*

The test on the Dreamliner was to "confirm adequate bonding and grounding where the wings join the fuselage on certain 787 Dreamliner airplanes". A Boeing employee witnessed some shenanigans, apparently saw the inspections not being performed or being done in a half-assed fashion and being logged as complete, and reported it to his supervisor. His supervisor reported it to executive leadership, and executive leadership reported it to the FAA who are investigating.

Boeing says that this will not affect the safety of planes in service, which I find a little dubious - seems to me that every plane in service will need an inspection. They also say that it will affect "customers and employees "because the test now needs to be conducted out of sequence on airplanes in the build process" i.e. they have to go back and redo those inspections, probably with additional supervision to make sure they're done properly and logged, which is going to disrupt production and slow down delivery for a little while.

Once again, corporate culture of 'gotta get them planes out the door to meet deliverables and quarterly profit expectations!' and not enforcing safety standards rears its ugly head.

https://arstechnica.com/tech-policy/2024/05/boeing-says-workers-skipped-required-tests-on-787-but-recorded-work-as-completed/
thewayne: (Default)
Care to guess who manufactured the plane?

The flight landed in Medford, Oregon Friday morning and a ground crew member noticed that a chunk of exterior fuselage was missing. This was part of the lower section behind the landing gear and is not pressurized, so it did not affect the main cabin directly, though it probably affected the plane's aerodynamics and might have caused it to suck fuel more rapidly.

The plane is a 737-800, not a 737 Max series, I read that the plane is approximately 25 years old IIRC.

In this case, the crew did not notice the incident and no emergency was declared.

One person familiar with the aircraft maintenance system and industry said that the entire industry needs to be investigated from the ground up, not just Boeing. Apparently shenanigans are rife.

https://www.cnn.com/2024/03/15/us/united-airlines-panel-missing-oregon/index.html


In other Boeing aircraft news:
--In one flight, smoke was smelled coming from the rear of the plane. I don't believe any smoke detectors triggered, but it was reported by multiple people. An emergency was declared, the plane rerouted to Phoenix (IIRC) and the plane was evacuated. Emergency and service personnel could not find a source for the smell.
--In a much rougher incident, a flight suffered an abrupt movement, not turbulence, in the middle of its flight, catching people off-guard and causing several injuries and some people being taken to the hospital. The plane went into an abrupt, somewhat steep dive, throwing some people into the ceiling. Important reason to wear your seat belt when at your seat! It would appear the pilot was getting out of his seat and something caused his seat to move in an uncontrolled fashion and hit the control yoke. Ambulances and emergency crew met the aircraft when it landed, some people were treated at the scene, some were taken to hospital. No deaths. Boeing has sent out an advisory for airlines to inspect the control cabin seats. NY Post says a flight attendant might have accidentally pushed a button on the pilot's seat that powered the captain's chair into the control yoke, causing the dive. The flight was en route to New Zealand and landed safely.

It should be noted that air safety for this year - even with that door plug blow-out - has been completely normal. Boeing is under a microscope - as they should be, so we're seeing a lot of louder coverage of anything involving Boeing aircraft and there are lots of them out there, which results in lots of coverage. Lots of things go wrong with planes on a regular basis, they're still amazingly reliable means of conveyance.

Boeing clearly has major problems and is going to be taken to task for it. We shall see what the final result is, but that is going to take some time, and the resolution of that will take even longer.
thewayne: (Default)
Wow. Words absolutely fail me.

John Barnett had worked for Boeing for thirty years before retiring in 2017 for medical reasons. He was a senior quality control engineer on the 787 program. He became a whistleblower when he saw sub-standard parts being installed and later discovered a 25% failure rate in the passenger breathing mask system for the 787.

He was in Charleston as part of a long-running legal battle against Boeing. When he failed to appear as part of this on Saturday, they searched for him at his hotel and he was found dead in his truck in the parking lot.

Of a self-inflicted gunshot wound to the head.

I really, REALLY hope the FBI steps in on this one. It might have been a clean suicide, it might not have been. But there's too much going on with Boeing without there being a VERY serious investigation into this!

https://www.bbc.com/news/business-68534703
thewayne: (Default)
Things were looking slightly up for them when they announced the possible acquisition of Spirit AeroSystems (I may have called it Spirit Aerospace in previous posts), the maker of their fuselages. Spirit was formerly their own company, but in a brilliant move they spun it off into its own company, leaving them with zero control to remediate manufacturing defects before the tubes were shipped from Kansas to Seattle/Tacoma for assembly, requiring a "warranty crew" to be permanently stationed at the Boeing plant to fix them up.

Not a smart move.

In the last couple of weeks we've seen these Boeing jet lovelies:
--A wheel fall off one of its rear landing wheel assemblies on take-off, causing a lot of damage to parked cars. Fortunately no one was injured. A similar thing happened a month or two ago where a jet was waiting to taxi for take-off, and a nose wheel decided to roll away.
--Another jet, on landing, lost function of its rudder, greatly affecting its ability to steer. The front wheel, while steerable, is not intended to steer the plane at speed, but in an emergency - as this kinda was - it can be used as such and the plane made it safely to the gate. Later testing found a failed component

Now, as terrible as a wheel falling off is, those aren't Boeing's fault. That's problems with the individual airline's maintenance. The failure of the rudder system? Same thing. Part failure, maintenance not noticing it. Not Boeing's fault. Not good optics, but that's just bad luck.

But that isn't the biggie. The Department of Justice has opened a criminal investigation into the January 5th Alaska Airlines door blowout incident.

Here is a particularly damning line in the article: "Boeing has acknowledged in a letter to Congress that it cannot find records for work done on the door panel of the Alaska Airlines plane." They cannot find records for work done on the door panel. What the ever-loving fuck. Aircraft repairs have log after log after log. Individual parts have logs noting how many hours are on them. Well, maybe not parts, but certainly assemblies. Boeing's computer systems REQUIRE that this stuff be logged! And they can't find the records.

This might be a good time to short Boeing stock

https://apnews.com/article/boeing-ntsb-door-plug-emergency-landing-2d23408a25eff999579c88071836dbec
thewayne: (Default)
Ed Clark had been in charge of the Max program for almost three years. He came up through the ranks and had been with Boeing for 18 years, having previously been chief engineer and chief 737 mechanic. He knows the plane.

This is purely sacrificial, a move by the board to appease investors. There was also a shuffling of directors and the creation of a new director position. See: Titanic and deck chair rearrangement. If they don't stop putting shareholder return above safety, it's not going to do a damn thing to improve the situation. Clark was not the reason those bolts weren't there, it was the board's drive for money by more rapidly pushing the planes out the door and increasing deliverables. Also a crappy ticketing system.

And this is what the board is trying to appease: "Beyond the problems that have resulted in the grounding of the 737 Max 8 and Max 9 after the incidents, the problems at Boeing have also postponed certification of two new versions of the jet, the Max 7 and a stretched version, the Max 10.

The CEOs of three key Boeing customers – United Airlines, Southwest and Delta Air Lines – have recently all said they no longer are counting on getting those new versions of the planes they had ordered anytime soon. United CEO Scott Kirby referred to the Alaska Air incident as the “straw that broke the camel’s back” in terms of his airline’s planning assumptions for the Max 10."
Southwest's entire fleet is almost 100% 737. They did this to standardize maintenance operations. If Southwest is willing to break that up, that's seriously bad news for Boeing.

https://www.cnn.com/2024/02/21/business/boeing-removes-head-of-737-max-program-in-wake-of-safety-incidents/index.html

https://tech.slashdot.org/story/24/02/24/0553215/boeing-removes-head-of-its-737-max-program-after-januarys-door-bolts-incident
thewayne: (Default)
Not much to say, really. If something had caused the door to pop out and the bolts were in-place, these stop fittings are supposed to arrest the bolts' vertical movement. There would be evidence in those fittings of stopping the movement, either scratches or deformation or something.

And 'tweren't there.

"Overall, the observed damage patterns and absence of contact damage or deformation around holes associated with the vertical movement arrestor bolts and upper guide track bolts in the upper guide fittings, hinge fittings, and recovered aft lower hinge guide fitting indicate that the four bolts that prevent upward movement of the MED [mid exit door] plug were missing before the MED plug moved upward off the stop pads."

https://arstechnica.com/tech-policy/2024/02/four-bolts-were-missing-from-boeing-737-before-door-plug-blew-off-ntsb-says/
thewayne: (Default)
Oh, boy! LUCY, YOU HAVE SOME 'SPLAININ' TO DO!

There are SOOO MANY problems here!

First off, the problem appears to be entirely Boeing's fault. Spirit manufactured the fuselage - including installing the door plug - then the fuselage was transported from Kansas to Seattle via train for final assembly. Okay, not unreasonable.

Except these fuselages are riddled with defects, or 'non-conformities'. Spirit has a team of technicians permanently based in Seattle to work on these at Boeing's assembly line. These are 'warranty repairs' by Spirit. No idea how big this team is, I expect pretty sizeable.

This particular fuselage, like all the others, had lots of problems. They immediately spotted a number of bad rivets on the door plug on the RIGHT side of the fuselage, but didn't spot problems on the door plug on the LEFT side, which was the one that blew out. They then discovered problems with the plug on the left side.

Now two other things need to be explained.

First, Boeing has two computer systems to deal with repair ticketing. One is used to broadly discuss issues, the other is used to specifically ticket the issue, and more particularly, mark when it's done. And hey, guess what! The two systems do not talk to each other! And it takes time to update tickets in the second system, and since we know companies do not like paying overtime, this sometimes doesn't happen.

This failure to update tickets is definitely a factor in the door plug blow-out.

The second thing to explain is a matter of basic physics, specifically, atmospheric pressure. At ground level, the air is much denser. The higher you climb, pressure is lower. Think about an airplane. It's pressurized. That means that as it climbs, the pressure on it decreases, and it's going to expand.

Now we're back to the door plug. And, for that matter, the doors on an aircraft. I'm definitely going to try to remember to look at this the next time I fly! The door plug is not welded in place, it's removeable, just like an emergency exit door is. It's just that it's not removeable from the inside - normally - without that trim panel being taken out first. To overly simplify it, bolts are screwed into the side of the plug. The head of the bolt sticks out. On the side of the aircraft, in the nook where the plug is, are these little guide tracks. As the plane gains altitude, the door plug actually slides up a little bit - but this isn't a problem as the guide tracks hold the plug in place. And pressurization isn't a problem because there's an excellent rubber seal around the door plug to maintain the cabin pressure.

Of course, this assumes that the bolts are in place. No bolts, nothing for the guide tracks to catch. And when the plane gets to a high enough altitude, the door plug goes sailing.

Boeing removed the door to service it - NOT SPIRIT. And they screwed the pooch when they reinstalled it. The bolts were not put back in place. It was not documented, and apparently when the door was recovered from that teacher's back yard, there were no bolts in the door.

The whistle-blower provided full documentation to the Seattle Times, and presumably the National Transportation Safety Board, as to what happened from Boeing's internal systems.


This article is a long read, but pretty understandable.

https://www.seattletimes.com/business/boeing-aerospace/boeing-not-spirit-mis-installed-piece-that-blew-off-alaska-max-9-jet/

https://news.slashdot.org/story/24/01/25/0314242/boeing-not-spirit-mis-installed-piece-that-blew-off-alaska-max-9-jet
thewayne: (Default)
Good news for Alaska Airlines and United Airlines. Alaska says they're going to resume some of their canceled flights Friday: it takes a little time to notify pilots and crew that they're needed back on the job.

HOWEVER....

"United Airlines chief executive, Scott Kirby, also told CNBC that he is "disappointed".
"The Max 9 grounding is probably the straw that broke the camel's back for us," he said, adding that "we're going to build a plan that doesn't have the [Boeing] Max 10 in it"."


Not that it will happen, but it's been suggested that Boeing should purge ALL McDonnell-Douglas executives that are still in the company and get actual engineers back into important positions. But it won't happen.

https://www.bbc.co.uk/news/business-68090175
thewayne: (Default)
Raise your hands if you're utterly shocked at this report.

[looks around, doesn't see a lot of hands raised]

The CEO of Alaska made a couple of interesting statements, but the most interesting was that they are reconsidering an order placed with Boeing for 277 MAX10 aircraft, which do not exist yet. Alaska recently purchased Hawaiian Air, which operates Airbus jets, I would imagine that Alaska is considering diversifying their fleet with an additional influx of Airbus. While this would increase their maintenance costs, it would probably help them in the long run.

Alaska is having to cancel approximately 150 flights a day while its MAX9 fleet is grounded, the FAA has not yet announced what it will take to get those jets back in the air.

https://www.nbcnews.com/business/business-news/alaska-airlines-found-more-loose-bolts-boeing-737-max-9-ceo-says-rcna135316

https://arstechnica.com/cars/2024/01/alaska-airlines-says-it-found-many-loose-bolts-on-its-boeing-737-max-9s/


In other news today, a nose wheel on a Boeing 757 fell off. Now, I'm not picking on Boeing on this one because the 757 is a much older jet. The plane was sitting on the ground waiting to taxi, and for reasons unknown, one of the two nose wheels decided it wanted to roll down a hill. There were no injuries to passengers or crew, and no further damage to the aircraft. Everyone deplaned, were put on another flight, and all was well. Large aircraft have two nose wheels, losing one was certainly unusual, but didn't represent a huge danger to the craft.

But there's an interesting note in this article. The travel service Kayak has added a filter that, when you're scheduling air travel, you can EXCLUDE Boeing 737 MAX aircraft! Now that is both useful and a huge PR blow to Boeing.

https://www.theguardian.com/business/2024/jan/24/delta-air-lines-plane-nose-wheel-falls-off


Boeing's problem is they fully embraced Wall Street culture when they merged with McDonnell-Douglas. They started chasing 'shareholder value' rather than its engineering/safety culture that it had before. Now it has the classic 'do more with less' which leads to corners being cut, and we can now clearly see what it's led to.

Airbus, on the other hand, even though it is making planes in the USA, is adhering to European safety standards and isn't seeing problems like this. While their planes aren't 100% perfect, they do something that I think is absolutely brilliant: the cockpit of each Airbus model is almost identical to every other! This minimizes pilot retraining and helps them get certified across types much more quickly. Boeing? Each one is its own beast, requiring its own multi-million dollar simulator and training program, and a lengthy training and certification program for pilots.
thewayne: (Default)
The airlines, while inspecting their grounded 737-MAX9 fleets, have reported finding loose bolts (United) and 'parts' (Alaska). Fortunately these are easily fixed by the maintenance crews. But it does lead you to ask WTF?! is going on at Boeing and the other company that is outfitting these planes!

No report on what other airlines are finding. But clearly Boeing's inspections are failing bigly.

Boeing stock lost 8% of its value Monday and more on Tuesday, unspecified in the article.

https://www.theguardian.com/world/2024/jan/08/united-finds-loose-bolts-boeing-737-max-planes
thewayne: (Default)
I've been waiting for some more information before writing about this, as it's quite the story!

If you have a fear of flying, maybe you don't want to read this. I am going to cut to the good news: no serious injuries and no one died. I'll put the rest under a cut for your consideration.

Read more... )
thewayne: (Default)
*SMH* Why didn't they just buy or lease the damn thing?

The company suing Boeing, Wilson Aerospace, is suing Boeing for theft of intellectual property. Wilson makes a special torque wrench, the Fluid Fitting Torque Device-3, which is ideal for monster bolts and high torque specifications in hard to reach places, such as inside a rocket booster assembly. Boeing needed such a device desperately to properly attach the engines to the SLS rocket. So they asked Wilson to come out for a demonstration. Little did they know that seven or more alleged Boeing employees were actually engineers for Wilson competitors who engaged in a hands-on demo, who went on to build a wrench for Boeing.

I really wish the article listed dollar amounts involved, I can't imagine paying competitors to develop the equivalent device was less expensive than buying or leasing it from the people who invented it. And it's not like Boeing hasn't already wasted a billion dollars or more on this project.

And here's another thing: lawsuit. Discovery process. So much is going to come out of this discovery process that will make Boeing look like absolute idiots that Fox News is going to be looking at them saying "See! We're not the only idiots out there!"

https://arstechnica.com/space/2023/06/supplier-sues-boeing-over-alleged-theft-of-sls-rocket-tools/

May 2025

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